湘军 发表于 2023-11-28 21:37

奥的斯ACD系列通用最新故障码(下)

使用服务器M1-1-2-1查看到的所有故障记录,所有事件类别分为I/W/F/E
IInformation信息
WWaring警告
FFault错误
E
Elite - Visible only in the ALL Menu Event Trace

savedRuns从上次送电到现在的运行次数
savedMins从上次送电到现在的时间(单位:分钟)

故障代码故障名称类别故障解释相关设置

System
0600 SPB-Alert W服务面板检测到一个错误,需要手动救援SPB 和 SDI。可能的原因有:SDI 的错误的速度编码器SPB 上缺陷的 E2PROMSPB 上的电池缺失按SPB 按钮,REB+DDO 同时,以定位错误源控制板检测到 SPB 和 SDI 故障. Ssk 可能的原因有:1.编码器故障2.SPB 上的 E2 存储器故障3.电池故障同时按 SPB 上的 REB+DDO 定位故障原因Error # 1, encoder A failure (only ...AAA/...AAB)Error # 2, encoder B failure (only ...AAA/...AAB)Error # 4, E2Prom failureError # 5, battery failureError # 12, 3 encoder A failureError # 13, received out of range parameters fromTCBC/GECB /RCBII

0601SPB:TempHTSW服务面板过热。SPB-Temp
0602LwssServiceW称重板请求REM。参见称重板故障原因。称重系统请求服务

0603Aro ServiceWThe ARO subsystem (modified SPBC_III) requested “Request For Service” (REM). See AROsubsystem’s event logging for reason.

0604S/WChangedI软件变更。SCN 更改

0605Update S/W!F升级软件!要求更新 GECB 软件

0606SpbServiceWSPB 请求服务

0607/TUM1FTUM1 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)TUM1(1047)HWY-TYP
0608/TUM2FTUM2 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)TUM2(1048)HWY-TYP
0609/TDMFTDM missing after run at BOTTOM or active during standstill; (shallow pit: trig- ger modul contacts)TDM(1049)HWY-TYP
0610/TUPSFTUPS missing during run; (reduced overhead: trigger modul power supply)TUPS(1050)HWY-TYP

0611/TDPSFTDPS missing during run; (shallow pit: trigger modul power supply)TDPS(1051)HWY-TYP
0612SOS upFSafety Operated Switch Up triggeredSOSU(1054)HWY-TYP
0613SOS downFSafety Operated Switch Down triggeredSOSD(1055)HWY-TYP
0614PRBB BatLowWThe battery of the PRBB board is weak: During PowerOff, the battery only pro- vides power forless than 10 seconds.EN-PRBB=1
0615PCB CertiWThe PCB certification is not performed by using OEK PDA until the specified days expired. In orderthat this function is ap- plied, it should be set by OEK PDA. Note: only for Korea application

0616C-circuitFC-circuit does not work correctlyNote: only for MCS310C-CHK (704)
0617RBU-SelftstFSelftest of Rope Brake has failed (i.e. lasted longer than 5 seconds).Car is blocked until TCI/ERO is switched.RBTC (1029)RBTE (1028)
0618RBU-FaultFRope Brake has detected overspeed. Car is blocked until TCI/ERO is switched.RBTC (1029)RBTE (1028)
0619HWY-TYPFPlease refer to blinking message “LOPIT cfg!”Low Pit
0626DeepBatteryFLVA Switch or Evolux: Deep Discharge Protection switched off the OCB to pro- tect the batteries(voltage was < 40 VDC).GECB-LV DRV-TYP
0627LowBat waitFLVA Switch or Evolux: Enforced Battery ChargingGECB_LV DRV-TYP
0628 NoPowerWait F LVA Switch or Evolux: BatRun-T expired during blackoutGECB-LV DRV- TYPBatRun-T
0629HighBatWaitFLVA Switch: Enforced Battery Discharg- ingBattery voltage exceeded 70 VAC.GECB-LV
0630OverBatFLVA Switch: Overvoltage Protection is going to switch off the OCB to protect the batteries(voltage > 75 VDC).GECB-LV
0631E2P MappedIThe LCB2/TCBC E2Prom data, provided by an E2TB (E2prom Transfer Board) were mapped to theGECB layout

event
0701 SP missing FNode Guarding does not detect the SP at the CAN bus. Check CAN_OK LED at SP;Check CAN wiring between GECB & SP;

0702 BCB missing FNode Guarding does not detect the 1st BCB at the CAN bus. Check CAN_OK LED at LVPB/BCB_IICheck CAN wiring between GECB & LVPB/BCB_II

0703 BcbIoFail FThe state of inputs was not received eve- ry second or the output command was not acknowledged.CAN bus overload?Defect LVPB/BCB_II?

0704BcbHwFailFThe BCB published an EEPROM error.Exchange LVPB/BCB_II

0705 BcbSwFail FThe BCB published a task timing prob- lem.See subcode ‘x’ for detailsExchange LVPB/BCB_II according to subcode

0706 EncoderFail FThe rescue encoder generates no signals during a normal run. Check rescue encoder wiring;Replace rescue encoder or GECB_II;

0707 OCB fail FThe OCB auxiliary contacts are wired incorrectly. Check wiring to OCB;Check OCB;Check GECB_II inputs;

0708 Overspeed WThe measured rescue encoder speed is 15% faster than the nominal speed. The OS contact or the safeties could be acti- vated. MRO is prevented.Reset OS contact;Check Encoder / Speed parameter; SPEEDEncoder
0709 MRO_BRK Flt FA wrong voltage at the brake was detect- ed.That means that the brake could be unin- tentionally lifted during MRO. Check input MRO_BRK and wiring of the brakeCheck LVPB / Replace LVPBDO NOT PERFORM MRO!!! LVA
0710No BatteryFThe 1st BCB misses the rescue battery.Check RPS / battery

0711 BatTempErr WThe 1st BCB indicates that the battery cannot be charged, because the tempera- ture is out of range.Check battery temperature sensor

注:删除单个故障:服务器 GO ON 或者 GO BACK 选中将要删除的故障
SHIFT(蓝健) + 1 (ON) 然后 SHFIT + CLEAR (ENTER) 当前单个故障删除新版本有 M1-1-2-7菜单,代替了SHIFT(蓝健)+UP(2 )了解详细的清除主板故障步骤在公众号里找:奥的斯服务器查看主板故障清除故障
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